De-gassifying the RV fridge

Having a propane flame boiling a mix of water, ammonia, and hydrogen doesn’t exactly scream “safe, modern RV fridge” to me. So – time to make a change.
Years ago, I had a propane accident. Nothing major, but painful enough. The flame just brushed my leg for a second, and that was more than enough to leave a lasting impression. Ever since then, I’ve been uneasy around propane. So having a burner running 24/7 in the back of our fridge? Not ideal. In fact, we used to turn the fridge off every night – because who wants to wake up in a flaming inferno?
Honestly, gas-powered absorption fridges are a leading cause of RV fires. And frankly, given the technology we have now, they should’ve gone extinct long ago. But the RV industry seems to love selling us outdated, inefficient tech (looking at you, rooftop A/C units) – mostly because, well, they can.
We’ve got 1000W of solar feeding 400aH of LiFePO4 batteries – more than enough to support a modern 12V compressor fridge. But I couldn’t find one that fit our RV’s fridge cavity. So we went with the JC-Refrigeration kit, which replaces the old absorption cooling system with a 12V compressor setup.
While my husband and I are pretty handy with tools, this retrofit wasn’t exactly a walk in the park. Not because the JC-Refrigeration kit or its documentation was bad – quite the opposite – but because, as always, you never know what the RV manufacturer (Winnebago, in our case) decided to do on any given assembly day.
We disconnected the propane line and power, removed all the mounting screws… and the fridge still wouldn’t budge. The documentation mentioned that on some Winnebago models, there might be hidden screws under the roof vent. Up I went to check – nothing.
“Are you sure?” asked my husband. “The fridge still won’t move.”
So up again I went, flashlight in hand. Checked every nook and cranny. Still nothing.
Back on the ground – no movement.
“Give me the flashlight,” he said.
Great. I’d left it on the roof. Up again. Another look. Still nothing.
Turns out it was a 120V receptacle mounted half to the fridge, half to the wall. One of those tiny things that make projects like this just a bit more annoying than they need to be.
Then there was the final aluminum fin screw – rusted beyond recognition. Why on earth didn’t they use stainless steel? It had to be drilled out. There goes another 30 minutes.
Getting the fridge out was a near-impossible puzzle. Even with the sink’s fold-down side table removed, there wasn’t enough clearance. Mounting brackets on each side stuck out a full three inches. We had to remove those just to squeeze the fridge out – with barely an inch to spare.
Once the fridge was safely on the ground, removing the old cooling unit was relatively easy – only took about 30 minutes. We carefully cleaned the back of the fridge box, stripped out the old foam and thermal paste, and prepped the aluminum freezer plate with acetone.
Now for the tricky part: mounting the new cooling unit. Eight screws in the freezer, two in the fridge compartment – all of which needed to line up perfectly with the new unit’s mounting holes. You cannot drill new holes or you risk hitting coolant pipes.
So here’s the method: stand the fridge upright, insert the new unit, and wiggle it around until you can see the mounting holes from inside the freezer. Temporarily screw it in with self-tappers, lay the fridge down again, mark the chassis screw points, remove the screws, and then – thermal paste time.
We were worried the paste might cover the holes, so we tried using toothpicks to mark them – which made the cooling unit look like some mad science project. That didn’t work out, but thankfully we managed to keep the paste away from the holes. Also: don’t tighten the screws until all are in, or paste may ooze and cover the remaining holes.
Next step: foam in the cooling unit. Gloves highly recommended. You want the foam to fill every gap for proper insulation. After curing for two hours, we trimmed the foam and sealed the edges with aluminum tape for a cleaner look.
Final step (or so we thought): connect 12V power to the control unit and compressor.
But surprise – the compressor sticks out about an inch farther than the old unit. Not enough room to slide it back in the easy way. We had to twist, tilt, and heave the fridge over the sink and back into place. At 8PM. Tired. Hungry. Cranky.
Once in position, we rigged a pedestal out of an icebox and some boards to lift and align the fridge, reattached the brackets, and finally – the fridge was back in its home.
Connected the 12V again, took a deep breath, and flipped the switch.
It hummed. Success!
The fridge cooled from 87°F to 63°F in about 45 minutes – even with me sneaking peeks. Current draw is about 8A at 12V (~100W). With a 60% duty cycle, that averages to ~4.8A – or about 83 hours of runtime on our battery without solar input. That’s pretty solid.
And the best part? No more open flame heating mystery chemicals in the back of my RV.
Mission accomplished.









Michaela Merz is an entrepreneur and first generation hacker. Her career started even before the Internet was available. She invented and developed a number of technologies now considered to be standard in modern web-environments. She is a software engineer, a Wilderness Rescue volunteer, an Advanced Emergency Medical Technician, a FAA Part 61 (PPL , IFR) , Part 107 certified UAS pilot and a licensed ham . More about Michaela ..
Call me super impressed. Not only impressed with the success of the fridge replacement but impressed with the engaging and detailed description of the process. Thank you.